Thats is precisely why I got rid of my RFL, damn thing would stall all the time because it would leak so bad. Now it is worth noting that my RFL was used for awhile before I got it.
Brian, you will probably be able to fix yours with additional washers as your unit is pretty new. You should be able to open it with your fingers at idle but still should require a bit of force to do so. And, there definately should not be a vac leak at idle thru the BOV.
I do agree with Stazi in that it should not have mysteriously died. They are a pretty simple device. You could check the routing of the vac line that is attached to top to make sure it isn't kinked anywhere.
The fluttering sound you described... I have read that can be compressor surge due to excess pressure not being vented and and can shorten the life of the turbo.
Brian, you will probably be able to fix yours with additional washers as your unit is pretty new. You should be able to open it with your fingers at idle but still should require a bit of force to do so. And, there definately should not be a vac leak at idle thru the BOV.
Brian, you will probably be able to fix yours with additional washers as your unit is pretty new. You should be able to open it with your fingers at idle but still should require a bit of force to do so. And, there definately should not be a vac leak at idle thru the BOV.
yeah as far as I can tell it doesn't leak at idle. but i couldn't really tell last night as the fans where running at the time so I thought that it was but it really wasn't.
other then that it tends to idle alittle high but i believe that is because the maf is reading well at idle. I unplugged it last night at idle and it came right down. however it wasn't happy when I reved it up. I need to cut back the intake tube leading to the maf as its to long and the outlet sit almost inside the maf ...
Ryan, the BOV is on its way. Should be there in 2-3 days.
So now the rfl is back on and working perfectly and not leaking at all. .
Nope not at all, and I also did the zip lock bag with a rubber band test too and it didnt suck the air out.
So yours is then, try removing it and spread some oil over the actuator and re-install it, thats what it took for mine.
I dont have any washers now and it sealed, with the washers in it wasnt working or sealing. But that may have been cause of the larger fmic.