been busy since the moment I got home working on the car.
stock y-pipe and test pipe where reinstalled. I also wired up my LC-1 Wideband controller. Everything works as it should. I also placed the Apexi turbo timer display/controller on the dash and ran the wire into the dash. Now I either need to wire it up or tuck it up under he dash to have black98svt (Doug from Shelton) wire it up and rewire my alarm.
The problem of the right appears to be that the O2 sensor bung on the test pipe is not centered over the hole in the pipe. When I tried to install the sensor it would jam up, like the threads didn't match. But if all O2 sensors have teh same thread then that isn't the problem. But from looking it apears the bung alignment is off. So I need to buy some files are fix that tomorrow. Or maybe I can pull the test pipe again and drill it out ...
the other goal tomorrow it to tape up and organize the LC-1 wires and put the center console kick panels back in. However I need to pull the center console for the turbo time to get access to the parking brake switch ...
hopefully tomorrow after getting another quart of Ford "Honey" for the mtx, as its just slightly low, I hope to drive the car again tomorrow.
all the parts I ordered should be in tomorrow or thursday. So hopefully this weekend I can get those fuel system upgrades done.
stock y-pipe and test pipe where reinstalled. I also wired up my LC-1 Wideband controller. Everything works as it should. I also placed the Apexi turbo timer display/controller on the dash and ran the wire into the dash. Now I either need to wire it up or tuck it up under he dash to have black98svt (Doug from Shelton) wire it up and rewire my alarm.
The problem of the right appears to be that the O2 sensor bung on the test pipe is not centered over the hole in the pipe. When I tried to install the sensor it would jam up, like the threads didn't match. But if all O2 sensors have teh same thread then that isn't the problem. But from looking it apears the bung alignment is off. So I need to buy some files are fix that tomorrow. Or maybe I can pull the test pipe again and drill it out ...
the other goal tomorrow it to tape up and organize the LC-1 wires and put the center console kick panels back in. However I need to pull the center console for the turbo time to get access to the parking brake switch ...
hopefully tomorrow after getting another quart of Ford "Honey" for the mtx, as its just slightly low, I hope to drive the car again tomorrow.
all the parts I ordered should be in tomorrow or thursday. So hopefully this weekend I can get those fuel system upgrades done.
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