Yeah, so I switched it around. It is a little louder now. I tried to remove the recirc. hose and run the car. It runs like crap w/o the recirc. hose. So I put it back on, and it runs fine.
I helped "Sprayed" hightower his lights last night. We took mine to the parts store. On the way I spiked to 15 psi for like a second! It freaked me out. As I'm leaving the parts store and driving down the road, I hear this wierd noise. I'm thinking I broke the motor or something. It is running fine, and still making boost..no loud noise. It just had this exhaust leak sound. Well, I get home and take a look. The short jaunt to 15 was too much for the wastegate gasket. I can see a clear gap where it used to be. I pulled off the wastegate today and made new gaskets. Both the old ones fall out in a few pieces. Well anyone with the recirculated wastegate knows what a PITA it is to put on. One of the bolts got cross threaded on install so I have to tap it tomorrow. It is covered with soot, so I think it has been leaking exhaust since the install. I took the boost controller off, cause now I'm scared of breaking something. I got another nut and JB welded it to the top. I can now "unthread" the valve another 1/4" to hopefully get it lower. I hope this will get me closer to 8# all the way out, instead of the 10-12# as it was without the extra nut on top.
Rod