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#663718 06/14/03 01:36 PM
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Hey, I know cross-posting is bad, but this is also a 3L issue and I am going to start the thread in here for those people that don't peruse the Forced Induction forum.
BurritaSVT just blew his turbo 2.5L motor, and it sounds just like what happened to mine.
I've been trying to track this problem down since it happened to me and I had some coincidental things happen that enlightened me to its nature; I believe that I have a good theory on it. Here's what I wrote in the FI'd forum:

**
You have a 99 and that is significant. That makes 3 or 4 forced inducted 1999 model year 3L or 2.5L engines that have cracked pistons. What happened to your engine sounds very similar to what happened to my 3L a couple of weeks ago.
By comparison, Keysers engine is a 2000 and I suspect that they have updated pistons in them.
I have discovered that on 3L's in late 1999 they updated the pistons and the position of the piston rings is moved upward on the piston.
The upper compression ring is higher, the 2nd compression ring is higher, the oil control ring is thinner but remains in the same place. This means there is more space between the 2nd compression ring and the oil control ring and results in a thicker 2nd compression ring land.
I was discussing this with Keith at Streetflight when my pistons went and I am beginning to see a pattern here.
When you get the engine apart, take pictures of the broken pistons for me so I can compare.
I think what you will need to do is similar to what I did, replace your pistons with the later updated style. We should try to get a picture of a 99 2.5L piston and 2000 2.5L piston. It may turn out that the pistons in 99 and older duratechs are not strong enough and that FI'd cars are going to need to have the late 99 or 2000+ pistons.

HEY EVERYONE:
This is SERIOUS folks as there are going to be a lot more failures out there if this theory is confirmed with fact AND it's likely it isn't detonation causing it, its cylinder pressure!
I don't think the 2.5L SC'd vortech motors will have a problem, since I think its torque loads ~250's that may be doing it. All turbo cars and 3L S/C's beware.

Tom
**

Lets get some brainpower here and any more pictures or information on 99 and earlier pistons vs. late 99 and later pistons!


Former owner of '99 CSVT - Silver #222/2760 356/334 wHP/TQ at 10psi on pump gas! See My Mods '05 Volvo S40 Turbo 5 AWD with 6spd, Passion Red '06 Mazda5 Touring, 5spd,MTX, Black
#663719 06/14/03 03:39 PM
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Here ya go Tom....

Here is a pic of my new 1mm over bore 3L piston and my 98 2.5L piston from my SVT......hope it helps.....

:


2005 Ford F150 SuperCab FX4 1964 Chevrolet Impala SS 1998 CSVT: 354HP/328TQ @ 10 psi, now gone
#663720 06/14/03 04:14 PM
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Remember the 2000's do have a slightly smaller displacement and higher compression ratio. So it does seem reasonable that the pistons are different.

You guys are making me nervous about my little trip to AZ coming up...

But I don't need insane power, so maybe I can just turn the boost down a bit until I have another good run in the stock market to build another engine

TB


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#663721 06/14/03 06:33 PM
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FWIW......

Jame's (CustomCougars) piston had a similar problem, while running the SF kit. His however is a 2001 2.5L. It is unsure what was the cause of his failure.


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#663722 06/14/03 07:08 PM
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James' piston had marks in the top where it smacked the valves. Not the same thing.


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#663723 06/14/03 08:53 PM
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I'll leave it up top, at least until you get this all sorted out.

#663724 06/14/03 11:13 PM
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Originally posted by CougarGT:
FWIW......

Jame's (CustomCougars) piston had a similar problem, while running the SF kit. His however is a 2001 2.5L. It is unsure what was the cause of his failure.




It was also rumored that he was running 87 octane. As to the truths of these rumors, I am unsure.


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#663725 06/14/03 11:53 PM
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I'm sure he wasn't running 87 octane. Probably just a simple mistake in shifting or switching of the programs.


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#663726 06/15/03 05:22 AM
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Originally posted by Keyser:
Probably just a simple mistake in shifting



I did that recently... The S-AFC doesn't lie either.


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#663727 06/15/03 07:28 AM
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here's a pic you might want to share interest in... its from my 99 CSVT 2.5L no forced induction but it might help to your theory... cylinder #4


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#663728 06/15/03 02:05 PM
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That is a front-bank piston that went?

I had two of the front-bank pistons crack in the ring area, this is a different problem. The hole piston let go, so I don't know all the data on this.
It is interesting as Buckshot had two front-bank pistons go just like mine, and one of the Streetflight engine also had the middle front-bank piston crack a ring land just like mine. All the pistons that seem to be going for whatever reason are on the front bank.
I don't know what is causing that but I'd sure like to find out. That is just too big of a coincidence for me to accept.

Tom


Former owner of '99 CSVT - Silver #222/2760 356/334 wHP/TQ at 10psi on pump gas! See My Mods '05 Volvo S40 Turbo 5 AWD with 6spd, Passion Red '06 Mazda5 Touring, 5spd,MTX, Black
#663729 06/15/03 07:21 PM
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as soon as you find out what it is let me know.... cuz i was pissed to see this when i took the heads off. its jsut the 2.5L but still ford might be hiding something.


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#663730 06/16/03 04:18 PM
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I'm liking this theory...

I have a 2000 2.5L non-SVT short block sitting in my basement doing nothing... i'll pull a piston off it tonite or tomorrow and take some pics... no damage on it, but it should help to prove your theory...

also I can get a hold of a micrometer if you want to post measurements of the different ring land thickness and ring thickness themselves as well as piston pin height.... i just need to know the exact points you want me to measure


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#663731 06/16/03 04:57 PM
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Thanks! What I'm trying to find out is if the 2000 2.5L blocks also have the updated rings like the 3L's.

Procyon would probably know, but he isn't around here right now it seems.

Tom


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#663732 06/17/03 01:30 AM
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2.5L 2000 NON-SVT Piston. Let me know what you want me to measure and I'll do that to.



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#663733 06/17/03 02:23 AM
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Heres a pic of my 2001 3L piston....




Let me know if you would like any measurements.






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#663734 06/17/03 02:42 AM
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Originally posted by warmonger:
Thanks! What I'm trying to find out is if the 2000 2.5L blocks also have the updated rings like the 3L's.

Procyon would probably know, but he isn't around here right now it seems.


The upper & lower compression rings on the 2.49L piston moved up compared to the earlier 2.54L piston.

#663735 06/17/03 02:43 AM
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Ok I just came back from my brother in-law's mold making shop

My piston has a dome center, so all measurements are not from the dome but from the top of the outer rim... we layed the piston upside down on 2 machined blocks on a flat marble work surface... pulled out some funky guage that sits flat on the table and zeroed it on top of one of the machined blocks... because he's a mold maker he measured everything 3 times to ensure accuracy...

top of first ring .158
top of second ring .368
top of oil ring .606
top of piston pin hole .769
piston pin diameter .828 (using telescoping guage)

do the math and i'm sure you can figure it all out


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#663736 06/17/03 01:05 PM
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Originally posted by PuckPuck:
Ok I just came back from my brother in-law's mold making shop

My piston has a dome center, so all measurements are not from the dome but from the top of the outer rim... we layed the piston upside down on 2 machined blocks on a flat marble work surface... pulled out some funky guage that sits flat on the table and zeroed it on top of one of the machined blocks... because he's a mold maker he measured everything 3 times to ensure accuracy...

top of first ring .158
top of second ring .368
top of oil ring .606
top of piston pin hole .769
piston pin diameter .828 (using telescoping guage)

do the math and i'm sure you can figure it all out




"Mold"?? Does he make Cheese, or penicillin perhaps?
Lol I'm just having fun.



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#663737 06/17/03 01:17 PM
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Ok. We have several cases of 99 3L and 2.5L SVT pistons having broken ring lands.

We have several cases of detonation.
I'm willing to say that detonation is obviously going to blow any piston, but that doesn't explain what is happening here when you just have broken ring lands.
There are 3 cases I know of where 99 and earlier engines have failed with no sign of detonation, or running lean with only cracked ring lands to show for it.
We have buckshots engine that shows clear signs of detonation from the melted edges of the pistons, and BurrtaSVT saying he has a hole in the top which also sounds like detonation.

Why do some engines show no sign of detonation and have broken secondary compression ring lands and are all 99 and earlier?
The only thing I can think of is that some of the compressive load on the top ring pushes it against its support, which also pushes against the second ring and its support respectively. However on the pistons with the thin second ring support it is just not thick enough to hold the load if cylinder pressures go really high.
Any sign of light detonation probably kills it; leaving me to concluded that the early 99 and earlier pistons for all duratechs probably have VERY little resistance to detonation and should be avoided in a FI'd or highly tuned high compression 3L engine.

Procyon, I'm probably wrong somewhere here, but you're an engine engineer so give us your take?


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#663738 06/17/03 02:19 PM
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Originally posted by warmonger:
Originally posted by PuckPuck:
Ok I just came back from my brother in-law's mold making shop

My piston has a dome center, so all measurements are not from the dome but from the top of the outer rim... we layed the piston upside down on 2 machined blocks on a flat marble work surface... pulled out some funky guage that sits flat on the table and zeroed it on top of one of the machined blocks... because he's a mold maker he measured everything 3 times to ensure accuracy...

top of first ring .158
top of second ring .368
top of oil ring .606
top of piston pin hole .769
piston pin diameter .828 (using telescoping guage)

do the math and i'm sure you can figure it all out




"Mold"?? Does he make Cheese, or penicillin perhaps?
Lol I'm just having fun.






I'm French Canadian... therefore I am allowed to mispell words, and have my own flavor of funky english grammar oh and i'm sure you figured out he's a MOULD maker

Now onto serious issues. I know how many of you praise the extra 1.2 points of compression, however now if money is tight and you can't afford a new set of pistons for your 99 block being converted to a 3L, you may want to think about running a lower compression by opening up the combustion chamber (only slightly more $$ in machine work). I have always felt that 11.2:1 is a decent jump on stock internals for an engine designed to run 10:1 or lower. Sure you'll lose a little HP for running the lower compression, but at least you won't have a 150lbs paperweight.

I'm still interested in knowing if we can say that all blown pistons were in the front bank... then the next question is WHY? Maybe the water pump has something to do with it, now i'm not sure but, that is the only big difference from front to rear.


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#663739 06/17/03 03:30 PM
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Originally posted by warmonger:
Ok.
We have buckshots engine that shows clear signs of detonation from the melted edges of the pistons.






Didn't Buckshot have forged pistons??


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#663740 06/17/03 04:20 PM
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Originally posted by Dan Nixon:
Originally posted by warmonger:
Ok.
We have buckshots engine that shows clear signs of detonation from the melted edges of the pistons.






Didn't Buckshot have forged pistons??




Nope stock, but he had forged rods.


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#663741 06/17/03 10:31 PM
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Originally posted by PuckPuck:
Now onto serious issues. I know how many of you praise the extra 1.2 points of compression, however now if money is tight and you can't afford a new set of pistons for your 99 block being converted to a 3L, you may want to think about running a lower compression by opening up the combustion chamber (only slightly more $$ in machine work)




Oh my! Now that is an interesting proposition, wish I'd heard of this before.?.? Makes me want to pull my heads off right now. lol

Originally posted by PuckPuck:

I'm still interested in knowing if we can say that all blown pistons were in the front bank... then the next question is WHY? Maybe the water pump has something to do with it, now i'm not sure but, that is the only big difference from front to rear.




So far they are all front-bank pistons. Why, I have no idea yet though I have mulled over it for a while.


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#663742 06/18/03 01:57 PM
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I still contend that most if not all of these failures have been detonation induced.

buckshot and burrita's failures involved melted areas on the pistons, this is indicitive of excess heat (duh), which may be due to the knock sensor retarding timing from excessive low level detonation. The others, where the ring lands are broken, may not have had time to melt anything, and a good, but quick bit of detonation may have been enough to cause it.
Remember, that the ring lands are typically the weakest area of a piston, and especially on a hypereutectic cast piston. These are the areas most sensitive to detonation damage.

Granted, this is just educated speculation, but I don't think there is any reason to freak out thinking these pistons are junk or anything, they are just not designed to handle the detonation that a lot of you guys are flirting with on these high compression duratecs, whether that high compression is purely static, or is dynamic (ie NA or forced induction)
If you want to make a durable motor, you have to do your homework all the way through and not just at random points.

1) When you start planning the motor, think logically about what you plan to do with it, and choose an appropriate CR, including dynamic CR (dynamic CR= static CR+ CR related to added boost) Perhaps an 11.2:1 static CR really isn't a good idea in a daily driver that runs on pump gas . . .

2) When putting your motor together, make sure you understand how the parts are interacting. One thing that has concerned me (I have no idea how well founded these concerns are though) is using 2.5L heads on a 3L block, because I have no idea what you are doing to the "squish band" because of the difference in the cylinder bore on the 3L and the 2.5L that the combustion chamber on the head is designed for. An improper squish band, as well as any hot spots induced in the combustion chamber can have a huge affect on how and when detonation occurs. As for me, I honestly don't know jack about the details of the squish band, and I wouldn't touch it myself without several very long conversations with both piston and head engineers/manufacturers/designers.

3) You can do all of your assembly and porting and other hard part work exactly right, but if you bugger the tune, you are screwed just as quickly. I think we all know Rick's (buckshot) first failure was most definately caused by a bad tune (or a tune not done yet ) just becuase Rick got a bit impatient before he could get the tune done.
Fuel and timing maps are of the utmost importance both for making optimal power and keeping your car running safely and reliably. OEMs spend thousands of hours perfecting the tune for power, driveability, durability, and emissions for every single possible powertrain combination they offer; do you really think that a simple one shot deal with an SAFC on your local backroad with a very inexperienced engine tuner (you, or most everyone you know) is enough to ensure that you have things set up safely and for optimum power?
Take the time to do it right; there are so many alternative routes to arrive at a proper tune, there really is no excuse for not doing it right. And if I hear "money" as an excuse from anyone, I will beat you about the head neck and chest with a wideband O2 sensor. It will cost you a lot more money in the long run to not do it right the first time. Ask Rick how much his one little incident of impatience has cost him . . .

There is so much more, but this is the gist of it. Now go do your own homework, the info is out there, you just have to look for it, and learn how to discern the good from the bad.

Geez, why do my technical posts always turn into books???


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#663743 06/18/03 10:57 PM
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very well put...i plan on tuning mine to the T.....if i can just get around to droping it in....its been in the spare bedroom for months now just waiting..


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#663744 06/19/03 12:14 AM
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Thats all very well and good, and some of it is common knowledge on here.

I did tons of homework on my motor and I think in both N/A and F/I modes it has shown itself to be a winner.
I don't know as much about engines as you guys do, but I will say that I'm trying to get to the bottom of an obvious problem. Its ok to say we're running on the edge, but that doesn't explain why its always front bank #2 and #4 pistons that are getting blown, even if it is through detonation.

I'm ok with you saying that the pistons ring lands being broken are caused by light detonation, it explains it and its the best theory by far.
I would like to point out that detonation IS causing a compressive load by the way since the pressure from the charge burning is coming on before the piston goes through TDC.
I can easily see from my temp readings that I was spiking temps of 190+ F when I cracked my pistons before, and detonation is probably what caused it. Ok.
But why always front bank?
YOu also have to see that with the thinner ring land supporting the second compression ring on the earlier pistons that it has to be the weaker link, AND that may be why they are more 'light-detonation' sensitive.
This is the gist of why I will say to use later model pistons.

tom


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#663745 06/27/03 08:24 PM
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i would probably say that the newer pistons might be even more prone to this problem then less so.... having a higher ring pack (aka rings higher up on the piston) puts less beef between the combustion process and the rings. manufacturers use this to up the compression and to clean up emissions. that space between the top of the pistons and the top of the rings is notorious to have unburned fuel and hydrocarbons that can escape during the exaust stroke.

now if the newer pistons are a better casting with higher quality control then it may be a wash but i still belive the fact that the ring lands are thinner might agrivate this issue more then anything. it maybe the fast that less 2000 cars have a turbo that this isnt showing up


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#663746 06/27/03 08:34 PM
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cont from my last post...

the primary ring is going to observe the most punishment in a detonation type event. where exactly are the breaking? is it at the top, or between the ring lands? what do the cooling passages look like around the block? ive never had mine apart (or never studied pics close enough) to see what they look like, how big are the cooling passages around the 2 and 4 cylinder? are they smaller or more obstructive the the rest? also how hard would it be to add piston oil squirters to our cars? as this would take a significant amount of heat out of the pistons. (i know that 3.0 and 3.5 non turbo nissans can be upgraded, however the turbo cars came with them, so that may be why)... i dont know what about those two cylinders running lean as the are closer to the throttle body? (just talking out my ass, to see what can be dreamed up). also what was the mixture like (12:1, 13:1)?


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#663747 06/27/03 08:53 PM
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You've misunderstood the issue.

The ring is a little closer to the combustion, but it isn't the rings that are breaking, it is the metal support, the ring land for the rings that is cracking.
Typically in cases where there is no melting of the aluminum present, the support for the lower compression ring is the part that is breaking. This particular support is half the thickness on the mid 99 and earlier pistons. In late 99 and up, this area was doubled in thickness by shifting the two rings upward by a couple of milimeters.
This is why under whatever loads and/or detonation that are breaking the lands is more prevalent on the earlier pistons.

As far as the two front bank pistons going out, they are the two that are furthest from the TB.


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#663748 06/28/03 03:12 AM
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do you have a pic?

what i now understand is the second combustion rig land is the one that let go not actually the top land? would that stmt be correct? i had assumed it was the top land that had let go and that by moving the land up closer to the chamber it was going to excite the problem even more. however if its the second land that is causing the failure i can see what u mean as the 2 combustion ring land is half the thickness. that would be fixed (or better off) with newer pistons as they are much thicker in that area....

but this still sounds like a tuning issue more then anything (detonation) what was the air/fuel ratio? also you might want ti try a cooler thermostat if you havent already done so (seeing as i dont know all your mods)

in the mean time while we are still working this out.... all turbo owners might want to keep the boost low and the mixture rich just to be safe


-Y2K SVT- BORN 1/03/2000 DIED 02/29/2004
#663749 06/28/03 01:10 PM
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This isn't about me really, it is about a whole series of pre-2000 motors that have cracked these rings in a similar manner, whatever the cause. Obvious the safest thing is to tune the engine properly.

Second, its about the strangeness of the fact that every single piston failure I know of both pre and post 2000 has been front bank pistons, both melted ones and just cracked ones.
Detonation induced or not, I want to know why just the forward bank pistons are breaking and never the back banks.


The general consensus is that the cracked pistons suffered from very light detonation, not necessarily lean induced that introduced a load strong enough to crack the second/lower compression ring. In one case on my piston it cracked the support for the 2nd and 1st ring, though no rings have broken.
This seems to be more prevalent on the pre mid 99 pistons with the thinner ring land support on the 2nd compression ring because it is thinner than the late 99/2000+ pistons.
So far, no one has ventured any reasonable guess to the issue of prevalence on the front bank.


Former owner of '99 CSVT - Silver #222/2760 356/334 wHP/TQ at 10psi on pump gas! See My Mods '05 Volvo S40 Turbo 5 AWD with 6spd, Passion Red '06 Mazda5 Touring, 5spd,MTX, Black
#663750 06/28/03 07:11 PM
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It is common for boosted engine to break the ringland on the piston in between the top and second rings. At first, this seems a little strange. But the greatest loads are supporting the top ring, which is being pressed down by combustion pressure. The only thing stopping it is the ringland below it.

Yes - toplands can also break, but more from a thermal failure.

#663751 06/28/03 08:14 PM
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You're still missing the point.
The ring support between the second compression ring and the oil control ring is the one that is breaking. The one between the 1st and 2nd compression ring has broken, but not usually. The support between the oil control ring and the second compression ring is 1/2 the thickness of the support between the 1st and 2nd compression ring.
See pictures.



Former owner of '99 CSVT - Silver #222/2760 356/334 wHP/TQ at 10psi on pump gas! See My Mods '05 Volvo S40 Turbo 5 AWD with 6spd, Passion Red '06 Mazda5 Touring, 5spd,MTX, Black
#663752 06/29/03 06:03 AM
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Question?

where is the water pump pickup point? is it the front bank drivers side? what i really want to know is where is the last place the coolant is before its cycle back thru the radiator? and also where is the radiator out let point connected to? maybe the coolant is super heated by the time it gets to those cylinders


-Y2K SVT- BORN 1/03/2000 DIED 02/29/2004
#663753 06/29/03 10:04 PM
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That's a worthwhile though. Lets see if anyone can determine the coolant flow path and see if it bears any fruit.


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#663754 06/30/03 06:48 PM
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Hey I see there a good debate going here about pistons but I failed to tell ya'll that my number 1 piston was the one that melted on the exhaust side and I asuming from this weakened it instantly and appeared like someone took a punch and pounded it through the piston on the side under the top ring and bottom ring.

I'm curious to what temp is required to do this. My number two cylinder next to it had little pits on the same side appearing to be next to break down. I almost looks like when the piston reaches a certain temp small pieces metal in grain form melt and fall off the piston surface and leaves small pits. Number 3 piston suffered nothing smooth finish.

i nevered pulled off the other head yet.

I ran my car yesterday with an egt and my car idles when warm at about 450 Celcius and with 8 psi it reaches right at 700 celcius and with 10.5 psi it reaches 750 celcuis my greddy gauge has the red line starting at 900 celcius to 1200 celcius.

I also have the probe in number one header one inch from head since this is the hottest cylinder being it has longest run in the intake for heat.

I don't know if this has anything to do with it but I'm also runing 30%rubbing achohol and 70% water injection system too. Does achohol affect this too?


99 SVT #198 blk/blue Spec 3/quaife/stage 2 shafts T3/T4 fully built 3.0 ported heads water injec./intercooled 13.2 @ 107 mph clifford alarm and turbo timer koni struts H&R springs intercooler for sale
#663755 06/30/03 07:13 PM
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My 2 pistons failed in the rear bank.....


2005 Ford F150 SuperCab FX4 1964 Chevrolet Impala SS 1998 CSVT: 354HP/328TQ @ 10 psi, now gone
#663756 10/14/03 04:45 PM
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One thing that i think most people are negating are the effects of the cams on dynamic as well as cylinder filling/scavaging. On a high end car something as simple as a header change can bring the car into detonation because of the increased vacuum generated by negative exhaust pressure on the intake ports. So in order to determine what is the exact cause of these pistons splintering and going everywhere you need to know whats done to the car. Intake manifold/header/cat/exhaust/cam/porting.

If the heads have been home ported this is a huge factor. Home ported heads never flow anywhere close from port to port and often the combination of gasses have MANY rich/lean pockets then when left in stock port. There are so many variables. And i dont nessasarily think its pre 99 engines only that do this. Im not sure of all the factors in these engines yet. But need to take some pics of the top of the pistons as well as the cylinder head to find the rich/lean pockets in the chamber. and see if where those are are on the side where the lans are cracked/broken. Alot of lan damage is caused by the uneven heating of the piston. If one side expands more then the other and runs tighter on the ring it causes alot more stress.

Also what chamber is being used in general is important as well. Because of the quenching at the top of the head This also has alot to do with what detonates and what doesnt.

There has to be some specific modification that people are doing to cause this. Also anyone have the intake events/exhaust events on the svt and 2.5 l standard cam as well as whats on the 3.0l . I could drop these into some equations and figure out if the dynamics you guys are running are too high or not. If someone could supply me with the maf read outs with a dyno run and what that converts to in pounds of air thatd be great too.


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#663757 10/14/03 04:58 PM
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1382* is packing alot of heat. Most of the time you start to loose valve seats in production between 1300-1400 Thats really hot. The turbo zetecs are running much cooler mid to low 1200 in toms 400 whp t3/t4 hybrid.probably need more fuel or reduce boost or if it also can be caused by excessive retardation of timing. Could advance ignition timing if its been retarded signifigantly. Cant help but think youv got a little detonation going on. IMO anyways. i cant think of a case where your exhaust gasses should reach 900 degrees c 1652 degrees f is way too hot. You hit that and your engine is already gone


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#663758 10/14/03 11:40 PM
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My engine in N/A form used to run 800 Celsius at 6700 rpm! This was after it was dyno tuned into the correct 12.5:1 A/F at 6700 rpm. I ran it a bit leaner in the lower rpm range but as it got up in rpm the temp still would climb. These engines just run hotter and they are made of more advanced materials than the average ford pushrod motors.
Turbo Tom's zetec is turbo so he is probably using fuel to keep the mixture cooler.
I try to run 12:1 or 12.5:1 with my turbo unit right now.
The only modifications that most of these people have made to their motors is boost. Some cracked pistons without having a dyno tune, like me.
-The hand porting jobs can be hit or miss I agree.
-BTW, I used the same tuning before and after the intercooler on my car. BEFORE I put on the intercooler I cracked two pistons. I put new pistons in the motor and then carefully drove it to the dyno in AZ to get the intercooler fitted and dyno'd with A/F.
The very first run with the intercooler on it and THE EXACT SAME A/F curve as previously when I cracked the pistons!! I put down 300 wHP and the A/F was 12.5:1

Therefore, the problem was in high combustion pressures/temps and possible that threw the A/F off enough along with the excess heat to make light detonation or it was just plain too much pressure.

Since then I have been running 50% more boost and no problems that I know of.

All your points are good except that:
1. Duratecs in good tune run high combustion temps.
2. The 99 and earlier pistons are definitely a weaker design...we have the pictures of the two types of pistons to prove it.



Former owner of '99 CSVT - Silver #222/2760 356/334 wHP/TQ at 10psi on pump gas! See My Mods '05 Volvo S40 Turbo 5 AWD with 6spd, Passion Red '06 Mazda5 Touring, 5spd,MTX, Black
#663759 10/15/03 01:28 AM
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Well is there anyway you could give me some specs on these engines? I dont have one or id figure it out myself. Im looking for a replacement for my zetec. Kinda figuring out what i want. It detonated the diffrential and while the tranny was on the floor i decided to upgrade engines while i was at it. So while im figuring my choice thought id learn about there weaknesses and this was a good place to start.

SO if youv got like a big data sheet on compression ratio`s valve sizes port flow data and everything else i could figure out what i could figure out and see if any of it could help you all find the solution.


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#663760 07/20/04 12:05 AM
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Question for you all. Would I run into this problem if I have replaced my Rods and Pistons with Forged ones?

#663761 07/20/04 12:46 AM
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Most likly not...You may encounter this if you use an OE replacment aftermarket brand.


Lupe


3.0 SVT hybrid...all the fixens...Track/Race ready very soon!!!!!! 20,000 + miles
#663762 07/24/04 02:19 PM
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Hey what psi were you guys running and for how long before the pistons broke? Did you have the turbo for a while or just after it was running?


98 E0 SVT with some stuff
#663763 07/25/04 04:52 AM
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The non-revised pistons are not suitable for boost.

It is really that simple.


2000 SVT #674 13.47 @ 102 - All Motor! It was not broke; Yet I fixed it anyway.
#663764 07/26/04 03:28 PM
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I have maintained 8 psi for about 12,000 miles on a 98 with no problems.


98 3.0 svt: Sold
#663765 07/27/04 07:40 AM
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So a late model 3.0L duratec (production date 6/99) would have the thiker thing and in theory should be okay?

#663766 07/27/04 10:58 AM
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Originally posted by {Kontofosho}:
I have maintained 8 psi for about 12,000 miles on a 98 with no problems.




Then consider yourself lucky. I have pictures of broken ring lands from a cougar, a 3L (my own) and two 98 SVT's.


Former owner of '99 CSVT - Silver #222/2760 356/334 wHP/TQ at 10psi on pump gas! See My Mods '05 Volvo S40 Turbo 5 AWD with 6spd, Passion Red '06 Mazda5 Touring, 5spd,MTX, Black
#663767 07/27/04 05:01 PM
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Originally posted by DeltarMN:
So a late model 3.0L duratec (production date 6/99) would have the thiker thing and in theory should be okay?



I don't think so.

The 3L did not get the revised pistons until early in the 2000 model year. Though 2000 seems to be the bastard year for the 3L.

Pistons changed, heads/intakes changed, some had coil on plug, some had a combonation of parts. (clearing out the parts bins I guess??? )


Ideally a 2001+ oval port 3L is the best choice for any 3L build.
More "ideally" yet would be it's from an Escape/Tribute. (upgraded oil pan, pickup, P/S pump & pulley, new front cover, etc)


2000 SVT #674 13.47 @ 102 - All Motor! It was not broke; Yet I fixed it anyway.
#663768 11/03/04 03:23 PM
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Do we know how much the newer pistons can take? What about 03 04 stuff are there further revisions? What CR do the newer 3L have?


98 E0 SVT with some stuff
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