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Originally posted by mcfast: I had the same thing now for A few months. After a few test I think I found my problem. Test #1, Put in new spark plugs NGK IRIDUMS std gap 54 ran good for 3 weeks after that runing bad agan. Test #2, New spark plug wires, look at the plugs did not look good, gap to 40 ran good but I went ahead put in some new spark plugs MotorCraft AGSF32PPM thay do not make them any more I put in some replacement MotorCraft plug std gap 54, run good for a week after that runing bad agan. Test #3, So today I completely clean my IMRC and put in some new pulgs, AUTOLITE APP764 gap to 40 so far so good we will see in a couple weeks if she is still runing good I think I have a weak coil.
Week 8 still very good, but my cheap short shifter fall apart today, I just reweld the ball back on now it is better then stock and still worth the price.
SVT 99 #526 of 2760
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Originally posted by mcfast: I had the same thing now for A few months. After a few test I think I found my problem. Test #1, Put in new spark plugs NGK IRIDUMS std gap 54 ran good for 3 weeks after that runing bad agan. Test #2, New spark plug wires, look at the plugs did not look good, gap to 40 ran good but I went ahead put in some new spark plugs MotorCraft AGSF32PPM thay do not make them any more I put in some replacement MotorCraft plug std gap 54, run good for a week after that runing bad agan. Test #3, So today I completely clean my IMRC and put in some new pulgs, AUTOLITE APP764 gap to 40 so far so good we will see in a couple weeks if she is still runing good I think I have a weak coil.
Week 9 still running very good,and the short shiter is holding up.
SVT 99 #526 of 2760
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Originally posted by mcfast: Week 9 still running very good,and the short shiter is holding up.
Strange... I thought you were quite happy with it!
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Originally posted by timstour: Originally posted by mcfast: Week 9 still running very good,and the short shiter is holding up.
Strange... I thought you were quite happy with it!
He is canadian... cut him some slack.
2k silver svt #1721
Ignorance breeds stupidity..
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Originally posted by timstour: Originally posted by mcfast: Week 9 still running very good,and the short shiter is holding up.
Strange... I thought you were quite happy with it!
Am I happy with it, put after a week the ball fall of and could not shift, it was in 3 gear, I got to work not too far, it took about a hour to fix just rewelded it now it is better then stock and will not brake any more. For me it is still worth 45.00$ I do not mind working on my car and a lot times I like it.
SVT 99 #526 of 2760
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Originally posted by mcfast: Originally posted by timstour: Originally posted by mcfast: Week 9 still running very good,and the short shiter is holding up.
Strange... I thought you were quite happy with it!
Am I happy with it, but after a week the ball fall of and could not shift, it was in 3 gear, I got to work not too far, it took about a hour to fix just rewelded it now it is better then stock and will not brake any more. For me it is still worth 45.00$ I do not mind working on my car and a lot times I like it.
SVT 99 #526 of 2760
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Originally posted by mcfast: I had the same thing now for A few months. After a few test I think I found my problem. Test #1, Put in new spark plugs NGK IRIDUMS std gap 54 ran good for 3 weeks after that runing bad agan. Test #2, New spark plug wires, look at the plugs did not look good, gap to 40 ran good but I went ahead put in some new spark plugs MotorCraft AGSF32PPM thay do not make them any more I put in some replacement MotorCraft plug std gap 54, run good for a week after that runing bad agan. Test #3, So today I completely clean my IMRC and put in some new pulgs, AUTOLITE APP764 gap to 40 so far so good we will see in a couple weeks if she is still runing good I think I have a weak coil.
Week 10, what can I say so far so good. Car is running great! Shifter is holding up to.
SVT 99 #526 of 2760
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Note I have a friend, his 95 had original wires and at idle we kept hearing knocking noise from the firewall bank. As it revved up the missing was more noticeable. Found the wire spark plug end/boot was arcing inside tube. As a temporary fix/test spread silicon rubber on the sides of the boot and let cure for about 20 minutes. (Do let any of the fumes from silicon rubber get suck into the intake!) Not good for O2's That was two years ago and he's driving that way. IRMC it should be in the achieves, but I found my circuit board (connector pins where cracked). resoldered and haven't had it act up once. Note I never had codes even when it did fail to open. Also don't forget to lube. I finally placed a teaspoon size of yellow wheeling bearing grease on the gears. I put nylon 3/8" spacers between the IMRC and was able to reuse the original bolts. Beauty cover on, still working flawless. Did this last spring so knocking on wood it stays flawless. 54k miles probably need to be thinking about pulling the UIM inspecting how the normal build is progressing.
Paul 98 Mystique LS (07/97)
Paul
98 Mystique LS 2ea (07/97)(08/98)
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Originally posted by mcfast: I had the same thing now for A few months. After a few test I think I found my problem. Test #1, Put in new spark plugs NGK IRIDUMS std gap 54 ran good for 3 weeks after that runing bad agan. Test #2, New spark plug wires, look at the plugs did not look good, gap to 40 ran good but I went ahead put in some new spark plugs MotorCraft AGSF32PPM thay do not make them any more I put in some replacement MotorCraft plug std gap 54, run good for a week after that runing bad agan. Test #3, So today I completely clean my IMRC and put in some new pulgs, AUTOLITE APP764 gap to 40 so far so good we will see in a couple weeks if she is still runing good I think I have a weak coil.
Week 11, still running great! I think this will be my last post on this one, unless it starts running bad agan. knock on wood
SVT 99 #526 of 2760
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Good call!
I have had high load stumbling on my 2.5L for about a year now. No CEL. Plugs fine.
I reflowed the connector and motor connections on the IMRC PCB and now all is right with the world. We'll see if it holds up.
DFT
1998 Mystique LS
2.5l Duratec
Willow Frost
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