Tonight, I connected up the remaining hoses. I just purchased my 1/2 x 13 heli coil insert for the drive shaft cam to pull the pulley in alignment with water pump. However, since it is close to being in alignment, I thought I'd take it for a test drive. Started the car and it idled smooth. I held my breath when shifting it to drive since I also rebuilt the atx in this project. Shifted to drive and it engaged....smoothly. Shifted to reverse and it engaged smoothly. Drove it around the block and it drove NICE. Trans winding up in gears sound strong and clean. Shift was very smooth. Took it out on the highway and drove it up to 55. Trans shifted fine. Front end is tight and seems not to need an alignment (replaced the struts, control arms, bushings, etc also) I will take it to be checked since I have a lifetime alignment warranty. Checked for leaks and found none. The only problem that I found was that my high cooling fan does not come on. Low speed works fine but high does not.....I did purchase a relay and replaced it but it did not make any difference. So the only items left on this project is pull down the water pump acessory pulley so it is in exact alignment with pump and repair high speed cooling fan..

This note closes out this project!

Regards,
Bob


An ounce of prevention provides a pound of cure!