('96 SE v6 MTX w/122k mi)
Okay, so I cleaned the TB, found a vacuum line out of place (but i might have done it when i pulled the rubber off of the TB), reconnected it, checked all the connections underneath and the 02 sensors are both tight instead of rattling around like before, but still a check engine light. I think I can feel the engine loading up, so I am thinking its still running rich even though it thinks its running lean.
I originally pulled a 174/430 from the code reader from Murrays.
The IMRC got rebuilt about a year ago and I am assuming they replaced gaskets then, so they shouldn't be leaking. Any other places to look for a vacuum leak? Also, I used a "teflon safe choke cleaner" to clean the TB, is there anything else recommended to use that works better or gets further in?


96 Ford Contour SE MTX, SVT exhaust, KKM intake, SP Motorsports slotted rotors, KVR pads, SP5000s -Stereo sucks