You may remember that I just finished a ported 3L back in the spring...it died in August due to cam friction and a jumped timing chain. I didn't have the urge to port another head and I'm a bit "cam" shy, so I went full 3L this time.
The new one is a 2004 with fully functional COP. I moved over all my other hi-po stuff like headers, pro-flow maf, fidanza, etc.
Started up and ran like new instantly! Really quiet and smooth...ass kicking torque. To you NW guys....this is what I was doing while you ran up to Packwood.
here's some shots:
So the whole conversion went well, with the EGR tube being a bigger PITA than the COP. But all is not good....it looks like LKQ has sold me a motor with a bad head gasket or cracked head. I'm blowing white smoke at any touch of the throttle...seems like the water is disappearing.
We'll see where this leads, but if it is a head issue, I'll fix it and get back at it.
The new one is a 2004 with fully functional COP. I moved over all my other hi-po stuff like headers, pro-flow maf, fidanza, etc.
Started up and ran like new instantly! Really quiet and smooth...ass kicking torque. To you NW guys....this is what I was doing while you ran up to Packwood.
here's some shots:



So the whole conversion went well, with the EGR tube being a bigger PITA than the COP. But all is not good....it looks like LKQ has sold me a motor with a bad head gasket or cracked head. I'm blowing white smoke at any touch of the throttle...seems like the water is disappearing.
We'll see where this leads, but if it is a head issue, I'll fix it and get back at it.